Analysis of surface defects of aluminium components with hard anodized layers
Identifikátory výsledku
Kód výsledku v IS VaVaI
<a href="https://www.isvavai.cz/riv?ss=detail&h=RIV%2F00216305%3A26620%2F15%3APU115385" target="_blank" >RIV/00216305:26620/15:PU115385 - isvavai.cz</a>
Výsledek na webu
<a href="http://dx.doi.org/10.1016/j.engfailanal.2015.01.013" target="_blank" >http://dx.doi.org/10.1016/j.engfailanal.2015.01.013</a>
DOI - Digital Object Identifier
<a href="http://dx.doi.org/10.1016/j.engfailanal.2015.01.013" target="_blank" >10.1016/j.engfailanal.2015.01.013</a>
Alternativní jazyky
Jazyk výsledku
angličtina
Název v původním jazyce
Analysis of surface defects of aluminium components with hard anodized layers
Popis výsledku v původním jazyce
Final quality inspection regularly reveals surface defects on components after hard anodizing. The aim of the analysis was to identify the cause of the defects and unambiguously determine whether the defect is caused by the quality of the base material, manufacturing technology of the component, the heat treatment or by the final surface treatment technology (anodizing). Analysis of the chemical composition and hardness measurements were performed to eliminate the possibility of any errors during material selection and heat treatment process. The capillary test revealed two major defects and also small amount of minor defects. To determine cause of the defects, light and scanning electron microscopy including EDS chemical microanalysis was used. Detailed study of the major defect and EDS microanalysis of its interior confirmed existence of defect prior to coating formation. Further examination of the major defect and its surroundings led to conclusion, that the defect was formed during primary foundry processes when billet was manufactured.
Název v anglickém jazyce
Analysis of surface defects of aluminium components with hard anodized layers
Popis výsledku anglicky
Final quality inspection regularly reveals surface defects on components after hard anodizing. The aim of the analysis was to identify the cause of the defects and unambiguously determine whether the defect is caused by the quality of the base material, manufacturing technology of the component, the heat treatment or by the final surface treatment technology (anodizing). Analysis of the chemical composition and hardness measurements were performed to eliminate the possibility of any errors during material selection and heat treatment process. The capillary test revealed two major defects and also small amount of minor defects. To determine cause of the defects, light and scanning electron microscopy including EDS chemical microanalysis was used. Detailed study of the major defect and EDS microanalysis of its interior confirmed existence of defect prior to coating formation. Further examination of the major defect and its surroundings led to conclusion, that the defect was formed during primary foundry processes when billet was manufactured.
Klasifikace
Druh
J<sub>imp</sub> - Článek v periodiku v databázi Web of Science
CEP obor
—
OECD FORD obor
20506 - Coating and films
Návaznosti výsledku
Projekt
<a href="/cs/project/ED1.1.00%2F02.0068" target="_blank" >ED1.1.00/02.0068: CEITEC - central european institute of technology</a><br>
Návaznosti
P - Projekt vyzkumu a vyvoje financovany z verejnych zdroju (s odkazem do CEP)
Ostatní
Rok uplatnění
2015
Kód důvěrnosti údajů
S - Úplné a pravdivé údaje o projektu nepodléhají ochraně podle zvláštních právních předpisů
Údaje specifické pro druh výsledku
Název periodika
ENGINEERING FAILURE ANALYSIS
ISSN
1350-6307
e-ISSN
1873-1961
Svazek periodika
56
Číslo periodika v rámci svazku
1
Stát vydavatele periodika
GB - Spojené království Velké Británie a Severního Irska
Počet stran výsledku
7
Strana od-do
300-306
Kód UT WoS článku
000361832300030
EID výsledku v databázi Scopus
2-s2.0-84941996309