Improvement of the Robotic Workplace to Prevent a Collision
Identifikátory výsledku
Kód výsledku v IS VaVaI
<a href="https://www.isvavai.cz/riv?ss=detail&h=RIV%2F46709002%3A_____%2F21%3AN0000050" target="_blank" >RIV/46709002:_____/21:N0000050 - isvavai.cz</a>
Výsledek na webu
<a href="https://link.springer.com/chapter/10.1007/978-3-030-83594-1_21" target="_blank" >https://link.springer.com/chapter/10.1007/978-3-030-83594-1_21</a>
DOI - Digital Object Identifier
<a href="http://dx.doi.org/10.1007/978-3-030-83594-1_21" target="_blank" >10.1007/978-3-030-83594-1_21</a>
Alternativní jazyky
Jazyk výsledku
angličtina
Název v původním jazyce
Improvement of the Robotic Workplace to Prevent a Collision
Popis výsledku v původním jazyce
In the serial production of air filters for the truck brake system, an im-portant operation is to pick and place four emptied boxes of semi-finished products from the assembly space. This, due to the prescribed production cycle, must be done in one step. These emptied boxes cannot be locked and it is therefore not possible to define the position in advance. It is nec-essary to implement a specialized camera system. This system must reveal the different positions and shapes of these boxes. The current high de-mand for production cycle and the restriction of the robot's movement is the reason for scanning only one box from said four vision system. This can lead to dangerous collisions between the robot's gripper and the pick-up boxes. The article deals with the improvement of the robotic work-place so as to avoid the mentioned collisions. The modifications consist in supplementing the workplace with optical inspection gates, implementa-tion of a special algorithm in the robot system, superior control system of the production line and HMI visualization. The whole update is carried out with regard to the high safety standards and requirements of the auto-motive industry.
Název v anglickém jazyce
Improvement of the Robotic Workplace to Prevent a Collision
Popis výsledku anglicky
In the serial production of air filters for the truck brake system, an im-portant operation is to pick and place four emptied boxes of semi-finished products from the assembly space. This, due to the prescribed production cycle, must be done in one step. These emptied boxes cannot be locked and it is therefore not possible to define the position in advance. It is nec-essary to implement a specialized camera system. This system must reveal the different positions and shapes of these boxes. The current high de-mand for production cycle and the restriction of the robot's movement is the reason for scanning only one box from said four vision system. This can lead to dangerous collisions between the robot's gripper and the pick-up boxes. The article deals with the improvement of the robotic work-place so as to avoid the mentioned collisions. The modifications consist in supplementing the workplace with optical inspection gates, implementa-tion of a special algorithm in the robot system, superior control system of the production line and HMI visualization. The whole update is carried out with regard to the high safety standards and requirements of the auto-motive industry.
Klasifikace
Druh
D - Stať ve sborníku
CEP obor
—
OECD FORD obor
20204 - Robotics and automatic control
Návaznosti výsledku
Projekt
—
Návaznosti
I - Institucionalni podpora na dlouhodoby koncepcni rozvoj vyzkumne organizace
Ostatní
Rok uplatnění
2021
Kód důvěrnosti údajů
S - Úplné a pravdivé údaje o projektu nepodléhají ochraně podle zvláštních právních předpisů
Údaje specifické pro druh výsledku
Název statě ve sborníku
Advances in Mechanism Design III
ISBN
978-3-030-83593-4
ISSN
2211-0984
e-ISSN
—
Počet stran výsledku
5
Strana od-do
204-209
Název nakladatele
Springer
Místo vydání
Liberec
Místo konání akce
Liberec
Datum konání akce
4. 8. 2021
Typ akce podle státní příslušnosti
WRD - Celosvětová akce
Kód UT WoS článku
—